
I'm sure that was the general feeling at British Leyland -- owners of the MG brand -- in the seventies. After all, their cars were already designed. All that they needed to do was just keep building them and selling them.
I became certain of this after owning a 1972 MGB. There were a lot of very good things about this car. I'll list them if I can think of them.
It also had some pretty serious faults. One of the most severe was the convertible top design. The MGB Experience website pretty much sums it up:
The Brits never did quite get the hang of making a convertible top that is easy to lower and raise. Folks who own a Fiat or Volkswagen (or virtually anything else built outside the United Kingdom) who can simply flip two toggles and throw the top back don't know how fortunate they are. Proceeding under the assumption that lowering the top on an LBC is just as easy can produce disastrous results.
Another shortfall of the MGs was the draconion maintenance requirements.
I understand that maintenance is required, but the MG's requirements were a bit excessive. Most american cars built in this timeframe would run for 100k miles with nothing more than oil changes and maybe a fresh set of spark plugs. By comparison, the MGB required routine maintenance approximately every 30 feet.
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What finally convinced me that British Leyland had no engineers on staff was the layout of the choke cable. The fact that this car, built in 1972, still had a manual choke was bad enough, but this design would have any engineer in tears. I assumed that mine was just installed wrong, but no;
they meant for it to be that way. The cable itself is firmly fixed to a bracket underhood (bonnet?). The sheath around the cable is connected to the choke lever. When you pull the choke knob in the cockpit, the cable tries to unkink and, in the process, manages to actuate the choke.
It's like someone hooked it up wrong and it just happened to work, sort of. So they left it that way
for 18 years of production.